Wednesday, June 17, 2020

At Home With Josh Part 8: Lisp System Installation

In our last installment our intrepid adventurer had gotten the Interphase 2181 SMD controller running again, and had used it to do a low-level format of a gigantic 160mb Fujitsu hard drive. This left him with all the ingredients needed to put together a running LMI Lambda system, at least in theory.

Tapes and Tape Drives

I had intended to wait until I’d found the proper 9-track tape drive for the system before attempting to go through the installation process. As you might recall, the Qualstar drive I have on the system is functional but extremely slow; it takes several minutes to find and load tiny diagnostic programs from tape. As system installation requires copying 20-30 megabytes from tape (i.e. a lot of data), it seemed to me that doing an installation from the Qualstar would simply take too long to be practical.

But on the other hand, the drive was functional and it occurred to me that possibly it was just the SDU “tar” utility’s simplicity that might be causing the extremely slow transfer rate: if it was overly conservative in its reads from tape, on an unbuffered drive like the Qualstar it might end up being very inefficient. Maybe the “load” tool would be a bit more intelligent in its tape handling. Or perhaps not — but there’s no harm in trying, right? And while I’d tracked down a proper Cipher F880 tape drive, it would require waiting until the current quarantine was lifted to go and pick it up. I demanded instant gratification so off I went. Except…

Shiny new 9-track tapes!
Ok, they’re still twenty years old.
That’s pretty new!
The other pressing issue was one of tapes. I have a small pile of blank (or otherwise unimportant) 9-track tapes here at home but all of them were showing signs of shedding and none of them worked well enough for me to write out a complete Lambda Install tape. Despite a few cleaning passes, eventually enough oxide would shed off the tape to gum up the heads and cause errors. Clearly I would need to find some better tapes, so I hit up eBay and found a stack of 5 tapes, new-old stock (apparently from NASA). And waited patiently for them to arrive.

[About a week passes…]

The Actual Installation

With new tapes in hand I was finally able to write out the “Install” tape without errors. And thus, with my fingers crossed and a rabbit’s foot in my pocket I started the installation process. The “load” utility is used to set up new hard disks and can copy files to and from tape to do installation and maintenance tasks. Here’s a transcription of the operation:

SDU Monitor version 102 >> disksetup What kind of disk do you have? Select one of { eagle cdc-515 t-302 micro-169 cdc-9766 }: micro-169 >> /tar/load using 220K in slot 9 load version 307 (creating block-22 mini-label) (creating mini-label) Disk is micro-169 Loading "/tar/bigtape" Loading "/tar/st2181" Disk unit 0 needs to be initialized: Disk has no label, or mini-label is wrong. Create new unit 0 label from scratch? (y/n) y Creating lisp label from scratch. How many LAMBDA processors: 1 Type "?" for command list. load >

The initial steps above tell the SDU that I have a “micro-169″ disk (the 8-inch equivalent of the giant 14” Fujitsu I actually have installed). This is necessary to allow the load program to know the characteristics of the system’s disk. /tar/load is then executed and since it finds an empty disk, it sets up the disk’s label, the LMI’s equivalent of a partition table — information written to the beginning of the disk that describes the disk and slices the its space into partitions that can be used to hold files or entire filesystems. Even though this Lambda is a “2X2” system (with two LAMBDA processors) it would be a tight squeeze to run both of them in the the 160mb capacity of the drive, so for now I will only be running one of the two processors. Or trying to, anyway. (Oooh, foreshadowing!)

Continuing on:
load > install ***************************************************** The new backup label track number is 16340. Record this number and keep it with the machine. ***************************************************** Writing unit 0 label Using half-inch tape Installing track-0 disk driver ... copying 10 blocks from "/tar/disk" to "disk" copy done Tape-ID = "FRED gm 7/23/86 12:33:34 522520414 " File is "SDU5 3.0 rev 14"; 1500 blocks. "SDU5 3.0 rev 14" wants to be loaded into UNX6. reading 1500 blocks into UNX6. copying 1500 blocks from "bigtape" to "UNX6" copy done Next file ... File is "ULAMBDA 1764"; 204 blocks. Default partition to load into is LMC3 reading 204 blocks into LMC3. copying 204 blocks from "bigtape" to "LMC3" copy done Next file ... File is " 500.0 (12/8)"; 23189 blocks. Default partition to load into is LOD1 reading 23189 blocks into LOD1. copying 23189 blocks from "bigtape" to "LOD1" copy done Next file ... End of tape. Writing unit 0 label load >

There are three tape files that the install process brings in; you can see them being copied above. The first (“SDU5 3.0 rev 14”) contains a set of tools for the SDU to use, diagnostics and bootstrap programs. The second (“ULAMBDA 1764″) contains a set of microcode files for use by the Lambda processor. The Lambda CPU is microcoded, and the SDU must load the proper microcode into the processor before it can run. The final file (cryptically named ” 500.0 (12/8)” is a load band. (The Symbolics analogue is a “world” file). This is (roughly) a snapshot of a running Lisp system’s virtual memory. At boot time, the load band is copied to the system’s paging partition, and memory-resident portions are paged into the Lambda’s memory and executed to bring the Lisp system to life.


As suspected the tape drive’s throughput was higher during installation than during diagnostic load. But not by much. The above process took about two hours and as you can see it completed without errors, or much fanfare. But it did complete!

Time now for the culmination of the last month’s time and effort: will it actually boot into Lisp? Nervously, I walk over to the LMI’s console, power it on, and issue the newboot command:
The “newboot” herald, inviting me to continue…

Newboot loaded right up and prompted me for a command. To start the system, all you need to do is type boot. And so I did, and away it went, loading boot microcode from disk and executing it, to bring the Lisp system in from the load band. Then the breaker tripped. Yes, I’m still running this all off a standard 15A circuit in my basement, and the addition of the Fujitsu drive has pushed it to its limit. Don’t do this at home, people.

I unplugged the tape drive to reduce the power load a bit, reset the breaker and turned the Lambda on again. Let’s have us another go, shall we?

(I apologize in advance for the poor quality of the videos that follow. One of the side-effects of being stuck at home is that all I have is a cellphone camera…)

(Warning, the above video is long, and also my phone gave out after 3:12. Just watch the first 30 seconds or so and you’ll get the gist of it.)

Long story short: about two minutes after the video above ended, the screen cleared. This normally indicates that Lisp is starting up, and is a good sign. And then… nothing. And more nothing. No disk activity. I gave it another couple of minutes, and then I pinged my friend Daniel Seagraves, the LMI expert. He told me to press “META-CTRL-META-CTRL-LINE” on the keyboard (that’s the META and CTRL keys on both the left and right side of the keyboard, and the LINE key, all held down at once). This returns control to the SDU and to newboot; at this point the “why” command will attempt to provide context detailing what’s going on with the Lambda CPU:


Tell me why, I gotta know why!

Since Daniel knows the system inside and out, he was able to determine exactly where things were going off the rails during Lisp startup. The error being reported indicated that a primitive operator expected an integer as an operand and was getting some other type. This hints at a problem inside the CPU logic, that either ended up loading a bogus operand, or that reported a valid operand as having a bogus type.

Out of superstition, I tried rebooting the system to see if anything changed but it failed identically, with exactly the same trace information from “why.”

In the absence of working diagnostics, schematics, or even detailed hardware information, debugging this problem was going to be an interesting endeavor.

But all was not lost. This is a 2×2 system, after all. There’s a second set of CPU boards in the chassis just waiting to be tested…


This time, after the screen clears (where the video above starts) you can see the “run lights” flashing at the bottom of the screen. (These tiny indicators reflect system and CPU activity while the system is running). Then the status line at the bottom loaded in and I almost fell over from shock. Holy cow, this thing is actually working after all this time!

I have one working Lambda CPU out of the two. I’m hoping that someday soon I can devise a plan for debugging the faulty processor. In particular, I think the missing “double-double” TRAM file opined about in Part 6 of this series has turned up on one of the moldy 9-track tapes I rescued from the Pennsylvania garage — this should hopefully allow me to run the Lambda CPU diagnostics, but it will have to wait until I have a larger disk to play with, as this file resides in a UNIX partition that I don’t currently have space for.

In the meantime since I have a known working set of CPU boards (recall from Part 2 that the Lambda processor consists of four boards), it was a simple matter to isolate the fault to a single board by swapping boards between the sets one at a time. The issue turns out to be somewhere on the CM (“Control Memory”) board in CPU 0.

Meanwhile, not everything is exactly rosy with CPU 1… what’s with the system clock?


System beeps are high-pitched squeaks and the wall clock on the status line counts about 4x faster than it should. Daniel and I are unsure exactly what the cause is at this time, but we narrowed it down to the RG (“ReGisters”) board. In many systems there is a periodic timer, sometimes derived from the AC line frequency (60Hz in the US) that is used to keep time and run the operating system’s process scheduler. The LMI uses something similar, and clearly it is malfunctioning.

Another fairly major issue is the lack of a working mouse. Way back in Part 2 I noted that the RJ11 connector had corroded into a green blob. This still needs repair and as it turns out, getting a working mouse on this system ended up being a journey all its own…

But that’s for my next installment. Until then, keep on keepin’ on!

Lookin’ good, LMI. Lookin’ good.


At Home With Josh Part 7: Putting the “Mass” in “Mass Storage”

Continuing from the conclusion of my last post, I had gotten to the point of testing the LMI’s Interphase SMD 2181 disk controller, but was getting troubling looking diagnostic output:
SDU Monitor version 102 >>/tar/2181 -C Initializing controller 2181: error 3 test 0 Alarm went off - gave up waiting for IO completion 2181: error 3 test 0 Alarm went off - gave up waiting for IO completion 2181: error 10 test 0 no completion (either ok or error) from iopb status iopb: cyl=0 head=0 sector=0 (TRACK 0) 87 11 00 00 00 00 00 00 00 00 00 00 10 00 c5 62 00 40 00 00 00 00 c5 3a
My immediate suspicion was that this was truly indicating a real failure with the controller. The “gave up waiting for IO completion” message was the canary in the coal mine here. The way a controller like this communicates with the host processor (in this case the SDU) is via a block of data in memory that the controller reads, this is the “iopb” (likely short for “I/O Program Block”) mentioned in the output above. The iopb contains the command to the controller, the controller executes that command then returns the status of the operation in the same iopb, and may interrupt the host processor to let it know that it’s done so. (More on interrupts later.)

What the above diagnostic failure appears to be indicating is that the SDU is setting up an initialization command in the iopb and waiting for the 2181 to return a result. And it waits. And it waits. And it waits. And then it gives up after a few milliseconds because the response has taken too long: the 2181 is not replying, indicating a hardware problem.

But the absence of any real documentation or instructions for these diagnostics or the 2181 controller itself left open other possibilities. The biggest one was that I did not at that time have an actual disk hooked up to the controller. The “-C” option to the 2181 diagnostic looked like it was supposed to run in the absence of a disk, but that could be an incorrect assumption on my part. It may well be that the 2181 itself requires a disk to be connected in order to be minimally functional, though based on experience with other controllers this seemed to me to be unlikely. But again: no documentation, anything could be possible.

The lack of a disk was a situation I could rectify. The Lambda’s original disk was a Fujitsu Eagle (model M2351), a monster of a drive storing about 470mb on 10.5″ platters. It drew 600 watts and took up most of the bottom of the cabinet. At the time of this writing I am still trying to hunt one of these drives down. The Eagle used the industry-standard SMD interface, so in theory another SMD drive could be made to work in its stead. And I had just such a drive lying dormant…

If the Eagle is a monster of a drive, its predecessor, the M2284 is Godzilla. This drive stores 160MB on 14″ platters and draws up to 9.5 Amps while getting those platters spinning at 3,000 RPM. The drive itself occupies the same space as the Eagle so it will fit in the bottom of the Lambda. It has an external power supply that won’t, so it’ll be hanging out the back of the cabinet for awhile. It also has a really cool translucent cover, so you can watch the platters spinning and the heads moving: 

The Fujitsu M2284, freshly installed in the Lambda.

The drive is significantly smaller in capacity than the Eagle, but it’s enough to test things out with. It also conveniently has the same geometry as another, later Fujitsu disk that the SDU’s “disksetup” program knows about (the “Micro-169”), which makes setup easy. I’d previously had this drive hooked up to a PDP-11/44 and was working at that time. With any amount of luck, it still is.

Only one thing needed to be modified on the drive to make it compatible with the Lambda — the sector size. As currently configured, the drive is set up to provide 32 sectors per track; the Lambda wants 18 sectors. This sector division is provided by the drive hardware. The physical drive itself provides storage for 20,480 bytes per track. These 20,480 bytes can be divided up into any number of equally sized sectors (up to 128 sectors per track) by setting a bank of DIP switches inside the drive. Different drive controllers or different operating systems might require a different sector size.

The 32 sector configuration was for a controller that wanted 512-byte sectors — but dividing 20,480 by 32 yields 640. Why 640? Each sector requires a small amount of overhead: among other things there are two timing gaps at the beginning and end of each sector, as well as an address that uniquely identifies the sector, and a CRCs at the end of the sector. The address allows the controller to verify that the sector it’s reading is the one it’s expecting to get. The CRC allows the controller to confirm that the data that was read was valid.

What a single sector looks like on the Fujitsu.




The more sectors you have per track, the more data space you lose to this overhead. The Lambda wants 1024-byte sectors, which means we can fit 18 sectors per track. 20,480 divided by 18 is approximately 1138 bytes — 114 bytes are used per sector as overhead. The configuration of the DIP switches is carefully described in the service manual: 

Everyone got that? There will be a quiz later. No calculators allowed.

Following the instructions and doing the math here yields: 20,480 / 18 = 1137.7777…, so we truncate to 1137 and add 1, yielding 1138. Then we subtract 1 again (Fujitsu enjoys wasting my time, apparently) and configure the dip switches to add up to 1137. 1137 in binary is 10 001 110 001 (1024 + 64 + 32 + 16 + 1), so switches SW1-1, SW1-5, SW1-6, SW1-7 are turned on, along with SW2-4. Simple as falling off a log!

With that rigamarole completed, I hooked the cables up, powered the drive up and set to loading the Interphase 2181 diagnostic again:

SDU Monitor version 102
>>/tar/2181 -C
Initializing controller
2181: error 3 test 0 Alarm went off - gave up waiting for IO completion
2181: error 3 test 0 Alarm went off - gave up waiting for IO completion
2181: error 10 test 0 no completion (either ok or error) from iopb status
iopb: cyl=0 head=0 sector=0 (TRACK 0)
87 11 00 00 00 00 00 00 00 00 00 00 10 00 c5 62 00 40 00 00 00 00 c5 3a

Darn. Looks like having a drive present wasn’t going to make this issue go away.

About that time, a local friend of mine had chimed in and let me know he had a 2181 controller in his collection. It had been installed in a Sun-1 workstation at some point in its life, and was a slightly different revision. I figured that if nothing else, comparison in behavior between his and mine might shed a bit of light on my issue so I went over to his house to do a (socially distanced) pickup.

Annoyingly, the revisional differences between his 2181 and mine were fairly substantial:


Two Interphase 2181’s. Can YOU spot the differences?

You can see the commonality between the two controllers, but there are many differences, especially with regard to configuration jumpers — and since (as I have oft repeated) there is no documentation, I have no idea how to configure the newer board to match the old.

So this is a dead end, the revisional differences are just too great. I did attempt to run diagnostics against the new board, but it simply reported a different set of failures — though at least it was clear that the controller was responding.

Well it was well past the time to start actually thinking about the problem rather than hoping for a deus ex machina to swoop in and save the day. I wasn’t going to find another 2181, and documentation wasn’t about to fall out of the sky. As with my earlier SDU debugging expedition, it seemed useful to start poking at the 2181’s processor, in this case an Intel 8085. This is an 8-bit processor, an update of the 8080 with a few enhancements. Like with the SDU’s 8088, looking at power, clock and reset signals was a prudent way to start off.

Unlike with the SDU, all three of these looked fine — power was present, the clock was counting out time, and the processor wasn’t being reset. Well, let’s take a look at the pinout of the 8085 and see what else we might be able to look at:

8085 pinout, courtesy Wikimedia Commons (https://commons.wikimedia.org/wiki/File:Anschlussbelegung_8085.gif)



Oscillation overthruster
The AD0 through AD7 and A15 pins are the multiplexed address/data bus: When the 8085 is addressing memory, AD0-AD7 plus the A8-A15 pins form the 16-bit memory address; when a read or write takes place, AD0-AD7 contain the 8-bits of data being read or written. Looking for activity on these pins is a good way to see if the CPU is actually running — a running CPU will be accessing and addressing memory constantly — and sure enough, looking with an oscilloscope showed pulsing on these pins.

The TRAP, RST7.5, RST6.5, RST5.5, and INTR signals are used to allow external devices to interrupt the 8085’s operation and are typically used to let software running on the CPU know that a hardware event has occurred: a transfer has completed or a button was pushed, for example. When such an interrupt occurs, the CPU jumps to a specific memory location (called an interrupt vector) and begins executing code from it (referred to as an interrupt service routine), then returns to where it was before the interrupt happened. If any of these signals were being triggered erroneously it could cause the software running on the CPU to behave badly.

Probing the RST7.5, 6.5 and 5.5 signals revealed a constant 3.5V signal at RST7.5, a logic “1” — something connected to the 8085 was constantly interrupting it! This would result in the CPU running nothing but the interrupt service routine, over and over again. No wonder the controller was unable to respond to the Lambda’s SDU.

Now the question is: what’s connected to the RST7.5 signal? It could potentially come from anywhere, but the most obvious source to check on this controller is one chip, an Intel 8254 Programmable Interval Timer. As the name suggests, this device can be programmed to provide timing signals — it contains three independent clocks that can be used to provide precise timing for hardware and software events. The outputs of these timers are often connected to interrupt pins on microprocessors, to allow the timers to interrupt running code.

The Intel 8254 Programmable Interrupt Timer
And, as it turns out, pin 17 (OUT 2) of the 8254 is directly connected to pin 7 (RST7.5) of the 8085. OUT 2 is the data output for the third counter, and goes high (logic “1”) when that timer elapses. Based on what I’m seeing on the oscilloscope, this signal is stuck high, likely indicating that the 8254 is faulty. Fortunately it’s socketed, so it’s easy to test that theory. I simply swapped the 8254s between my controller and the one I’m borrowing from my friend and…

Success! Probing RST7.5 on the 8085 now shows a logic “0”, the CPU is no longer constantly being pestered by a broken interval timer and is off and running. The diagnostic LEDs on the board reflect this change in behavior — now only one is lit, instead of both. This may still indicate a fault, but it’s at least a different fault, and that’s always exciting.

Well, the controller is possibly fixed, and I already have a disk hooked up and spinning… let’s go for broke here and see if we can’t format the sucker. The “-tvsFD” flags tell the controller to format and test the drive, doing a one-pass verify after formatting. Here’s a shaky, vertically oriented video (sorry) of the diagnostic in action:


And here’s the log of the output:
SDU Monitor version 102 >> reset >> disksetup What kind of disk do you have? Select one of { eagle cdc-515 t-302 micro-169 cdc-9766 }: micro-169 >> /tar/2181 -tvsFD Initializing controller 2181: status disk area tested is from cyl 0 track 0 to cyl 822 track 9 2181: status format the tracks Doing normal one-pass format ... 2181:at test 0 test reset passed 2181: test 1 test restore passed 2181: test 2 test interrupt passed failedginning of cyl 159 ... at beginning of cyl 0 ... 2181: error 18 test 4 header read shows a seek error iopb: cyl=0 head=0 sector=0 (TRACK 0) 00 00 82 12 00 00 00 00 00 00 00 12 10 00 c5 62 00 40 00 00 00 00 c5 3a 2181: error 18 test 4 header read shows a seek error The 1 new bad tracks are:... bad: track 1591; cyl=159 head=1 ... mapped to track 8229; cyl=822 head=9 There were 1 new bad tracks Number of usable tracks is 8228 (822 cyls). (creating block-10 mini-label) Disk is micro-169 2181: test 5 read random sectors in range passed 2181: status read 500 random sectors 2181: test 6 write random sectors in range passed 2181: status write to 500 random sectors 2181: test 8 muliple sector test passed 2181: test 9 iopb linking test passed 2181: test 10 bus-width test passed 2181: test 0 test reset 0 errors 2181: test 1 test restore 0 errors 2181: test 2 test interrupt 0 errors 2181: test 4 track verify 2 errors 2181: test 5 read random sectors in range 0 errors 2181: test 6 write random sectors in range 0 errors 2181: test 8 muliple sector test 0 errors 2181: test 9 iopb linking test 0 errors 2181: test 10 bus-width test 0 errors >>
And some video of the drive doing its thing during the verification pass:



As the log indicates, one bad track was found. This is normal — there is no such thing as a perfect drive (modern drives, both spinning rust and SSD have embedded controllers that automatically remap bad sectors from a set of spares, providing the illusion of a flawless disk). Drives in the era of this Fujitsu actually came with a long list of defects (the “defect map”) from the factory. A longer verification phase would likely have revealed more bad spots on the disk.

Holy cow. I have a working disk controller. And a working disk. And a working tape drive. Can a running system be far off? Find out next time!

Tuesday, June 16, 2020

At Home With Josh Part 6: Diagnostic Time!

In our last exciting episode, after a minor setback I got the Lambda’s SDU to load programs from 9-track tape. Now it’s time to see if I can actually test the hardware with the available diagnostics.
Tape Images

Tape images of the Lambda Release and System tapes are available online. Daniel Seagraves has been working on updating the system and has his latest and greatest are available here. A tape image is a file that contains a bit-for-bit copy of the data on the original tape. Using this file in conjunction with a real 9-track drive allows an exact copy of the original media to be made. In my case, I have an HP 7980S 9-track drive connected to a Linux PC for occasions such as these. At the museum we have an M4 Data 9-track drive set up to do the same thing. The old unix workhorse tool “dd” can be used to write these files back to tape, one at a time:

$ dd if=file1 of=/dev/nst0 bs=1024

(Your UNIX might name tape devices differently, consult your local system administrator for more information.)

Data on 9-track tapes is typically stored as a sequence of files, each file being separated by a file mark. The Lambda Release tape contains five such files, the first two being relevant for diagnostics and installation, and the remainder containing Lisp load bands and microcode that get copied onto disk when a Lisp system is installed.

The first file on tape is actually an executable used by the SDU — it is a tiny 2K program that can extract files from UNIX tar archives on tape and execute them. Not coincidentally, this program is called “tar.” The second tape file is an actual tar archive that contains a variety of utility programs and diagnostics. Here’s a rundown of the interesting files we have at our disposal:
  • 3com – Diagnostic for the Multibus 3Com Ethernet controller
  • 2181 – Diagnostic for the Interphase 2181 SMD controller
  • cpu – Diagnostic for the 68010 UNIX processor
  • lam – Diagnostic for the Lambda’s Lisp processors
  • load – Utility for loading a new system: partitioning disks and copying files from tape.
  • ram – Diagnostic for testing NuBus memory
  • setup – Utility for configuring the system
  • vcmem – Diagnostic for testing the VCMEM (console interface) boards.
The unfortunate thing is: there is no documentation for most of these beyond searching for strings in the files that might reveal secrets. Daniel worked out the syntax for some of them while writing his LambdaDelta emulator, but a lot of details are still mysterious.

In case you missed it, I summarized the hardware in the system along with a huge pile of pictures of the installed boards in an earlier post — it might be helpful to reacquaint yourself to get some context for the following diagnostic runs. Plus pictures are pretty.

I arbitrarily decided to start by testing the NuBus memory boards, starting with the 16mb board in slot 9 (which I’d moved from slot 12 since the last writeup). The diagnostic is loaded and executed using the aforementioned tar program as below. The “-v” is the verbose flag, so we’ll get more detailed output. the “-S 9” indicates to the diagnostic that we want to test the board in slot 12.
SDU Monitor version 102 >> reset >> /tar/ram -v -S 9 ram: error 6 test 1 bad reset state, addr=0xf9ffdfe0, =0x1, should=0x4 ram: error11 test 3 bad configuration rom ram: error 1 test 6 bad check bits 0xffff, should be 0xc, data 0x0 ram: error 1 test 7 bad check bits 0xffff, should be 0xc, data 0xffffffff ram: error 7 test 8 for dbe w/flags off, DBE isn't on ram: error 7 test 9 for dbe w/flags off, DBE isn't on ram: status fill addr 0xf9000000 ram: status fill addr 0xf9002000 ... [elided for brevity] ... ram: status fill addr 0xf903c000 ram: status fill addr 0xf903e000 ram: status fill check addr 0xf9000000 ram: status fill check addr 0xf9002000 ... [elided for brevity] ... ram: status fill check addr 0xf903c000 ram: status fill check addr 0xf903e000
Well, the first few lines don’t look exactly promising what with all the errors being reported. The test does continue on to fill and check regions of the memory but only up through address 0xf907e000 (the first 512KB of memory on the board, that is). Thereafter:
ram: status fill check addr 0xf907c000 ram: status fill check addr 0xf907e000 ram: status block of length 0x4000 at 0xf9000000 ram: status stepsize 4 forward ram: error 4 test 16 addr 0xf9000004 is 0xffffffff sb 0x0 (data f/o) ram: error 4 test 16 addr 0xf9000008 is 0xffffffff sb 0x0 (data f/o) ram: error 4 test 16 addr 0xf900000c is 0xffffffff sb 0x0 (data f/o) ram: error 4 test 16 addr 0xf9000010 is 0xffffffff sb 0x0 (data f/o) ram: error 4 test 16 addr 0xf9000014 is 0xffffffff sb 0x0 (data f/o) ram: error 4 test 16 addr 0xf9000018 is 0xffffffff sb 0x0 (data f/o) ram: error 4 test 16 addr 0xf900001c is 0xffffffff sb 0x0 (data f/o) ram: error 4 test 16 addr 0xf9000020 is 0xffffffff sb 0x0 (data f/o) ram: error 4 test 16 addr 0xf9000024 is 0xffffffff sb 0x0 (data f/o) ram: error 4 test 16 addr 0xf9000028 is 0xffffffff sb 0x0 (data f/o)
And so on and so forth, probably across the entire region from 0xf9000000-0xf907ffff. This would take a long time to run to completion (remember, this output is coming across a 9600bps serial line — each line takes about a second to print) so I wasn’t about to test this theory. The output appears to be indicating that memory reads are returning all 1’s (0xffffffff) where they’re supposed to be 0 (0x0).

So this isn’t looking very good, but there’s a twist: These diagnostics fail identically under Daniel’s emulator. After some further discussion with Daniel it turns out these diagnostics do not apply to the memory boards I have installed in the system (or that the emulator simulates). The Memory boards that were available at the time of the Lambda’s introduction were tiny in capacity: Half megabyte boards were standard and it was only later that larger (1, 2, 4, 8, and 16mb boards) were developed. The only memory boards I have are the later 4 and 16mb boards and these use different control registers and as a result the available diagnostics don’t work properly. If there ever was a diagnostic written for these newer, larger RAM boards, it has been lost to the ages.

This means that I won’t be able to do a thorough check of the memory boards, at least not yet. But maybe I can test the Lisp CPU? I slotted the RG, CM, MI and DP boards into the first four slots of the backplane and started up the lam diagnostic program:

SDU Monitor version 102 >> reset >> /tar/lam -v /tar/lam version 6 compiled by wer on Wed Mar 28 15:24:02 1984 from machine capricorn setting up maps initializing lambda starting conreg = 344 PMR passed ones test passed zeros test TRAM-ADR passed ones test passed zeros test TRAM passed ones test passed zeros test loading tram; double-double disk timed out; unit=0x0 cmd=0x8F stat=0x0 err=0x0 disk unit 0 not ready can't open c.tram-d-d SPY: passed ones test passed zeros test HPTR: Previous uinst destination sequence was non-zero after force-source-code-word during lam-execute-r Previous uinst destination sequence was non-zero after force-source-code-word during lam-execute-r Previous uinst destination sequence was non-zero after force-source-code-word ... [and so on and so forth] ...
Testing starts off looking pretty good — the control registers and TRAM (“Timing RAM”) tests pass, and then it tries to load a TRAM file from disk. Aww. I don’t have a disk connected yet, and even if I did it wouldn’t have any files on it. And to add insult to injury, as it turns out even the file it’s trying to load (“double-double”) is unavailable — like the later RAM diagnostics, it is lost to the ages. The TRAM controls the speed of the execution of the lisp processor and the “double-double” TRAM file causes the processor to run slowly enough that the SDU can interrogate it while running diagnostics. Without a running disk containing that file I won’t be able to proceed here.

So, as with the memory I can verify that the processor’s hardware is there and at least responding to the outside world, but I cannot do a complete test. Well, shucks, this is getting kind of disappointing.

The vcmem diagnostic tests the VCMEM board — this board contains the display controller and memory that drives the high-resolution terminals that I restored in a previous writeup. It also contains the serial interfaces for the terminal’s keyboard and mouse. Perhaps it’s finally time to test out the High-Resolution Terminals for real. I made some space on the bench next to the Lambda and set the terminal and keyboard up there, and grabbed one of the two console cables and plugged it in. After powering up the Lambda, I was greeted with a display full of garbage!

Isn’t that the most beautiful garbage you’ve ever seen?
This may not look like much, but this was a good sign: The monitor was syncing to the video signal, and the display (while full of random pixels) is crisp and clear and stable. The garbage being displayed was likely due to the video memory being uninitialized: Nothing had yet cleared the memory or reset the VCMEM registers. There is an SDU command called “ttyset” that assigns the SDU’s console to various devices; currently I’d been starting the Lambda up in a mode that forces it to use the serial port on the back as the console, but by executing

>> ttyset keytty
The SDU will start using the High-Resolution terminal as the console instead. And, sure enough, executing this caused the display to clear and then:

It lives!

There we are, a valid display on the screen! The keyboard appeared to work properly and I was able to issue commands to the SDU using it. So even without running the vcmem diagnostic, it’s apparent that the VCMEM board is at least minimally functional. But I really wanted to see one of these diagnostics do its job, so I ran it anyway:
SDU Monitor version 102 /tar/vcmem -v -S 8 vcmem: status addr = 0xf8020000 vcmem: status fill addr 0xf8020000 ... [elided again for brevity] ... vcmem: status fill addr 0xf803e000 vcmem: status fill check addr 0xf8020000 vcmem: status fill check addr 0xf8022000 vcmem: status fill check addr 0xf8024000 vcmem: status fill check addr 0xf8026000 ... vcmem: status fill check addr 0xf8036000 vcmem: status fill check addr 0xf8038000 vcmem: status fill check addr 0xf803a000 vcmem: status fill check addr 0xf803c000 vcmem: status fill check addr 0xf803e000
As the test continued, patterns on the screen slowly changed, reflecting the memory being tested. Many different memory patterns are tested over the next 15 minutes.
vcmem: status movi block at 0xf803c000 vcmem: status movi stepsize 2 forward vcmem: status movi checking 0x0000 writing 0xffff vcmem: status movi checking 0xffff writing 0x0000 vcmem: status movi stepsize 2 backward vcmem: status movi checking 0x0000 writing 0xffff vcmem: status movi checking 0xffff writing 0x0000 vcmem: status movi stepsize 4 forward vcmem: status movi checking 0x0000 writing 0xffff vcmem: status movi checking 0xffff writing 0x0000 vcmem: status movi stepsize 4 backward vcmem: status movi checking 0x0000 writing 0xffff vcmem: status movi checking 0xffff writing 0x0000 vcmem: status movi stepsize 8 forward vcmem: status movi checking 0x0000 writing 0xffff vcmem: status movi checking 0xffff writing 0x0000 vcmem: status movi stepsize 8 backward vcmem: status movi checking 0x0000 writing 0xffff vcmem: status movi checking 0xffff writing 0x0000 ... [elided] ... vcmem: status movi stepsize 4096 forward vcmem: status movi checking 0x0000 writing 0xffff vcmem: status movi checking 0xffff writing 0x0000 vcmem: status movi stepsize 4096 backward vcmem: status movi checking 0x0000 writing 0xffff vcmem: status movi checking 0xffff writing 0x0000 vcmem: status movi stepsize 8192 forward vcmem: status movi checking 0x0000 writing 0xffff vcmem: status movi checking 0xffff writing 0x0000 vcmem: status movi stepsize 8192 backward vcmem: status movi checking 0x0000 writing 0xffff vcmem: status movi checking 0xffff writing 0x0000
And at last the test finished with no errors reported, leaving a test pattern on the display. How about that, a diagnostic that works with the hardware I have.

Not your optometrist’s eye chart…
Looking crisp, clear, and nice and straight. This monitor is working fine — what about the other one? As you might recall, I got two High-Resolution Terminals with this system and pre-emptively cleaned and replaced all the capacitors in both of them. The second of these would not display anything on the screen when powered up (unlike the first) though I was seeing evidence that it was otherwise working. Now that I’d verified that the VCMEM board was working and producing a valid video signal, I thought I’d see if I could get anything out of the second monitor.


Well, what do you know? Note the cataracts in the corners.

Lo and behold: it works! I soon discovered the reason for the difference in behavior between the two monitors: The potentiometer (aka “knob”) that controls the contrast on this display is non-functional; with it turned up on the first monitor you can see the retrace, with it turned down it disappears. Interestingly the broken contrast control doesn’t seem to have a detrimental effect on the display, as seen above.

So that’s a VCMEM board, two High-Resolution Terminals, and the keyboard tested successfully, with the CPU and Memory boards only partially covered. I have yet to test the Ethernet and Disk controllers. The 3com test runs:
SDU Monitor version 102 >> /tar/3com -v 3com: status Reading station address rom start addr=0xff030600 3com: status Reading station address ram start addr=0xff030400 3com: status Transmit buffer: 0xff030800 to 0xff030fff. 3com: status Receive A buffer: 0xff031000 to 0xff0317ff. 3com: status Receive B buffer: 0xff031800 to 0xff031fff. 3com: status Receive buffer A - 0x1000 to 0x17ff. 3com: status Receive buffer B - 0x1800 to 0x1fff. >>
Hex editors to the rescue!
No errors reported and the test exits without complaining so it looks like things are OK here. Now onto the disk controller. I don’t have a disk hooked up at the moment, but after a bit of digging into the test’s binary, it looks like the “-C” option should run controller-only tests:



SDU Monitor version 102 >>/tar/2181 -C Initializing controller 2181: error 3 test 0 Alarm went off - gave up waiting for IO completion 2181: error 3 test 0 Alarm went off - gave up waiting for IO completion 2181: error 10 test 0 no completion (either ok or error) from iopb status iopb: cyl=0 head=0 sector=0 (TRACK 0) 87 11 00 00 00 00 00 00 00 00 00 00 10 00 c5 62 00 40 00 00 00 00 c5 3a 2181: error 3 test 0 Alarm went off - gave up waiting for IO completion 2181: error 3 test 0 Alarm went off - gave up waiting for IO completion 2181: error 10 test 0 no completion (either ok or error) from iopb status iopb: cyl=0 head=0 sector=0 (TRACK 0) 87 11 00 00 00 00 00 00 00 00 00 00 10 00 c5 62 00 40 00 00 00 00 c5 3a 2181: error 3 test 0 Alarm went off - gave up waiting for IO completion 2181: error 3 test 0 Alarm went off - gave up waiting for IO completion 2181: error 10 test 0 no completion (either ok or error) from iopb status iopb: cyl=0 head=0 sector=0 (TRACK 0) 87 11 00 00 00 00 00 00 00 00 00 00 10 00 c5 62 00 40 00 00 00 00 c5 3a 2181: error 3 test 0 Alarm went off - gave up waiting for IO completion
This portends a problem. The output seems to indicate that the test is asking the controller to do something and then report a status (either “OK” or “Error”) and the controller isn’t responding at all within the allotted time, so the diagnostic gives up and reports a problem.

This could be caused by the lack of a disk, perhaps the “-C” option isn’t really doing what it seems like it should, but my hacker sense was tingling, and my thought was that there was a real problem here.

Compounding this problem is a lack of any technical information on the Interphase SMD 2181 controller. Not even a user’s manual. The Lambda came with a huge stack of (very moldy) documentation, including binders covering the hardware: “Hardware 1” and “Hardware 3.” There’s supposed to be a “Hardware 2” binder but it’s missing… and guess which binder contains the 2181 manual? Sigh.

There are two LEDs on the controller itself and at power-up they both come on, one solid, one dim. In many cases LEDs such as these are used to indicate self-test status — but lacking documentation I have no way to interpret this pattern. I put out a call on the Interwebs to see if I could scare up anything, but to no avail.

Looks like my diagnostic pass at the system was a mixed bag: Outdated diagnostics, meager documentation, and what looks like a bad disk controller combined with the success of the consoles and at least a basic verification of most of the Lambda’s hardware.

In my next installment, I’ll hook up a disk and see if I can’t suss out the problem with the Interphase 2181. Until then, keep on chooglin’.


At Home With Josh Part 5: Tape Drives and EPROMS And Whiskers on Kittens

After working on the Lambda’s monitors as described in my last writeup, my next plan of action was to see if I could get diagnostics loaded into the SDU via 9-track tape.

ROM Upgrade Time


SDU Monitor, Version 8
But first, I wanted to upgrade the SDU’s Monitor ROM set. The SDU Monitor is a program that runs on the SDU’s 8088 processor. It provides the user’s interface to the SDU where it provides commands for loading and executing files, and booting the system. It also communicates with devices on the Multibus and the NuBus. As received, my Lambda has Version 8 of the monitor which is as far as I know the last version released to the public at large. However, the Lambdas that Daniel Seagraves owns came with an internal-only Monitor in their SDUs, designated Version 102. This version adds a few convenient features: it can deal more gracefully with loss of CMOS RAM (important since I don’t have a backup battery anymore) and adds a few commands for defining custom hard drive types.


One of the 27128A EPROMs
A week or so prior, Daniel had sent me a copy of the Version 102 ROMs so all I had to do was write (“burn”) the copy onto real EPROMs and install them in the SDU. I had spare EPROMs (four Intel 27128A’s) at the ready but the thing about EPROMs is that they need to be erased before they can be programmed with new data. To do that, you need an EPROM eraser — a little box with a UV lamp in it and a timer — and after searching the house for mine, I came to the realization that I’d taken it to work a few months back for and I’d never brought it back home. And due to present circumstances, it was going to be stuck there for awhile.


Bah.

So with much wailing and gnashing of teeth I ordered a replacement off the Internet and began waiting patiently for it to arrive in 5-7 days. Meanwhile I decided to start documenting this entire process for some kind of blog thing and so I went off, took pictures, and started writing long-winded prose about Lisp Machines and restorations.

Also during this time I decided to test the old wives’ tale about using sunlight to erase EPROMs. At that time Seattle was experiencing an extremely lovely bout of sunny weather, so I took four 27128’s outside, put them on the windowsill so as to gather as much sun as possible, and left them there for the next four days.

[Four Days Pass…]

They’re still not erased. So much for that idea. Only a few more days until my real EPROM eraser arrives anyway…

[A Few More Days Pass…]



At last my dirt-cheap EPROM ERASER arrived on my doorstep bearing dire warnings of UV exposure and also of the overheating of this fine precision instrument. Ignoring the 15 minute time-limit warning, I put four EPROMs into the drawer, cranked the timer up to 30 minutes and turned it on. And once again I found myself waiting.

[Thirty Minutes Pass…]

The Faithful DATA I/O 280 Gang Programmer
I pulled out my trusty DATA I/O 280 programmer and ran its “blank check” routine to ensure that the EPROMs were indeed as blank as they ought to be, and the programmer said “BLANK CHECK OK.”

It’s then a simple matter to hook the programmer up to my PC and program the new ROMs and soon enough all four were ready to get installed in the SDU. But before I did that I wanted to double-check that the Lambda was still operating — it’d been a couple of weeks since I had last powered it up and things can go wrong sometimes. Best not to introduce a new variable (i.e. new ROMs) into the equation before I can verify the current state.

Uh Oh

And so I hooked things back up to the Lambda and turned it on. And… nothing. No SDU prompt on the terminal and all three LEDs on the front panel are stuck on solid. (As we learned in my second post in this series, this indicates that the SDU is failing its self tests.) I pressed the Reset button a couple of times. Nothing. Power cycled the system just for luck. NIL.

“Well, fiddle-dee-dee!” I said. (I may have used slightly more colorful language than this, but this is a family-friendly blog). “Gosh darn it all to heck.”

I retraced my steps — had I changed anything since the last time I’d powered it on? Yes — I’d installed an Ethernet board that Daniel had graciously sent me (my system apparently never had an Ethernet interface, which is an odd choice for a Lisp Machine). Maybe the Ethernet board was causing some problem here? Pulling the board made no difference in behavior. I checked the power supply voltages at the power supply and at the backplane and everything was dead on. I pulled the SDU out and inspected it, and double-checked socket connections and everything looked OK.

Well, at this point I’m frustrated and my tendency in situations like this is to obsess about whether I broke something and so I run in circles for a bit when what I really need to do is take a step back: OK — it’s broken. How is it broken? How do I go about answering that question? Think, man, think!

Well, I know that the three LEDs are on solid — this would indicate that the SDU’s self-test code either wasn’t running or wasn’t getting very far before finding a failure. So: let’s assume for now that the self-test code isn’t running — how do I confirm that this is the case?

The SDU uses an Intel 8088 16-bit microprocessor to do its business, and it’s a relatively simple matter to take a look at various pins on the chip to see if there’s activity, or lack thereof. The most vital things to any processor (and thus good first investigations while debugging a microprocessor-based system) are power, clock, and reset signals. Power obviously makes the CPU actually, you know, do things. A clock signal is what drives the CPU’s internal logic, one cycle at a time, and the reset signal is what tells the CPU to clear its state and restart execution from step 0. A lack of the first two or an abundance of the latter could cause the symptoms I was seeing.

i8088 pinout, from the datasheet.
Time to get out the oscilloscope; this will let me see the signals on the pins I’m probing. Looking at the Intel 8088 pinout (at right) the pins I want to look at are pin 40 (Vcc), Pin 21 (RESET) and pin 19 (CLK). Probing reveals immediately that Vcc and CLK are ok. Vcc is a nice solid 5 volts and CLK shows a 5Mhz clock signal. RESET however, is at 3.5V — a logic “1” meaning that the CPU is being held in a Reset state, preventing it from running!

So that’s one question answered: The SDU is catatonic because for some reason RESET is being held high. Typically, RESET gets raised at power-up (to initialize the CPU among other things) and might also be attached to a Reset button or other affordance. In the SDU, there is also power monitoring signal attached to the RESET line designated as DCOT (DC Out of Tolerance) — if the +5 voltage goes out of range the CPU is reset:





Power supply status signals, from the “SDU General Description” manual.

It seemed possible (though unlikely) that the Lambda’s Reset switch or the cabling associated with it had failed, causing the symptoms I was seeing, but as expected the cabling tested out OK.

SDU Paddlecard.
The cable carrying the DCOT signal
is the bundle 2nd from the right.
I then checked the DCOT signal and even though the power supply voltages were measuring OK, I was reading 8V on the DCOT pin at the paddleboard. 8V is high for a normal TTL signal (which are normally between 0 and 5V) and this started me wondering. When I disconnected the DCOT wire from the paddleboard, the DCOT signal measured at the power supply was 0V while the signal at the paddleboard remained at 8V… suggesting some sort of failure between the power supply and the SDU for this signal. It also explains the the odd 8V reading– it’s likely derived from a 12V source with a pull-up resistor; the expectation being that the DCOT signal from the power supply would normally pull the signal down further into valid TTL range.

But what could have failed here? Clearly the power supply itself thinks things are OK (hence the 0V reading there). The difference in reading at one end versus the other can really only point to a problem in the wiring between the power supply and the SDU paddleboard.

Connectors just above the power supply.
Connector on the left carries actual power,
connector on the right contains the
power supply status signals.
There is a small three-conductor cable that runs from the SDU paddlecard down to a connector just above the power supply (pictured at the right). A second three-conductor cable is plugged into this and runs to the power supply itself. Checking these signals for continuity revealed that none of the three wires were continuous from the SDU back to the power supplies. The cable from the connector to the power supply tested fine — so what happened to the cable that runs from the connector to the SDU?

I pulled out the power supply tray to get a look at the cabling, and one glance below the card cage revealed the answer:




Oh.

“Aw, nut bunnies,” I may have been heard to remark to myself. Those three wires had apparently been ripped from the connector (quite neatly, I might add) the last time I had pushed the power supply drawer back in. (Likely while I was taking pictures of the power supplies for my blog writeups…) Quite how it got caught on the tray I’m not sure.

This was easy enough to fix — the wires were reinserted into the pins, and the cable itself rerouted so it would hopefully never get snagged on the power supply tray again. I reconnected everything, held my breath and flipped The Switch one more time.

[Several long seconds pass…]

SDU Monitor version 8 CMOS RAM invalid >>
greeted me on the terminal. Yay. Whew.

New SDU Monitor, At Last

OK. So at last I’m back to where I’d started this whole exercise, after an evening of panic and frenzied investigation. What was it I was going to do when I’d started out? Oh yeah, I had these new SDU ROMs all ready to go, let’s put ’em in:

SDU Monitor version 102 >> >> help r usage: r [-b][-w][-l] addr[,n] w usage: w [-b][-w][-l] addr[,n] d x usage: x [-b][-w][-l] addr[,n] dev usage: dev reset usage: reset [-m] [-n] [-b] enable usage: enable [-x] [-m] [-n] init usage: init ttyset usage: ttyset dev setbaud usage: setbaud portnum baudrate disktype usage: disktype type heads sectors cyls gap1 gap2 interleave skew secsize badtrk disksetup usage: disksetup setdr usage: setdr name file [ptr] >>


Ah, much better. So now the SDU was functional and upgraded, and I was ready to move onto the next phase: running system diagnostics.

9-Track Mind

The SDU has the capability to run programs off of 9-track tape. This is how an operating system is loaded onto a new disk and it’s how diagnostics are loaded into the system to test the various components. The Lambda uses a Ciprico Tapemaster controller, which is normally hooked up to a Cipher F880 tape drive mounted in the top of the Lambda’s chassis.

Qualstar 1052 9-Track Tape Drive
My Lambda’s F880 was missing when I picked it up, but the Tapemaster should in theory be able to talk to any tape drive with a Pertec interface. I’m still trying to track down an actual F880 drive, but in the meantime I have one potentially compatible drive in my collection — a Qualstar 1052. This was a low-cost, no-frills drive when it was introduced in the late 1980s but it’s simple and well documented and best of all: it has no plastic or rubber parts, so no worries about parts of the transport turning into tar or becoming brittle and breaking off.

It’s also really slow. The drive has no internal buffer so it can’t read ahead, which means that depending on how it’s accessed it may have to “shoeshine” (reverse the tape, then read forward again) the tape frequently. But speed isn’t really what I’m after here — will it work with the Lambda or won’t it?

I have a tape containing diagnostics (previously written on a modern Unix system with a SCSI 9-track drive attached) ready to go. So I cabled up the Qualstar to the Lambda’s Pertec cabling (as pictured in the above photograph) and attempted to load a program from the tape using the “tar” program:
>> /tar/load
The tape shoeshined (shoeshone?) once (yay!) and stopped (boo!), and the SDU spat back:
tape IO error 0xD >>
Well, that’s better than nothing, but only barely. But what does IO error 0xD mean? The unfortunate reality is that there is little to no documentation available on the SDU or the associated diagnostics. But I do have the Ciprico Tapemaster manual, thanks to bitsavers.org:

Relevant snippet from the Ciprico Tapemaster manual

Error 0xD indicates a data parity error: the data being transmitted over the Pertec cabling isn’t making it from the drive to the Tapemaster intact, so the controller is signalling a problem. The SDU stops the transfer and helpfully provides the relevant error code to us.

So where are the parity errors coming from? It could be a controller fault but given this system’s history I decided to take a closer look at the cabling first. A Pertec tape drive is connected to the controller via two 50-pin ribbon cables designated “P1” and “P2.” While I’d previously checked the cables for damage, I hadn’t actually checked the edge connectors at the ends of the cables, and well, there you go:

Crusty Connectors


It’s cleaner now, trust me.
It’s a bit difficult to discern in the above picture but if you look closely at the gold contacts you can see that there’s greenish-white corrosion on many of them. Dollars to donuts that this is the problem. For cleaning out edge connectors like this, I’ll usually spray the insides with contact cleaner and then, to apply a bit of abrasion to the pins, I wipe a thin piece of cardboard soaked in isopropyl alcohol in and out of the slot. I used this technique here and pulled out a good quantity of crud and dirt, leaving the connector nice and clean. Or at least clean enough to function, I hoped. Rinse and repeat for the second Pertec cable and let’s try this again:

>> /tar/load
And the tape shoeshines once… and shoeshines again… and again… hm. Is it actually reading anything or is there some other problem and it’s just reading the same block over and over? Let’s let it run for a bit…


>> /tar/load no memory in main bus Initializing SDU SDU Monitor version 102 >>
No more parity errors, and the “load” program did eventually load. It then complained about a lack of memory. It looks like the tape drive, the cable, and the controller all work! (Thanks to the Qualstar’s slowness, it took about five minutes between the “/tar/load” and the “no memory in main bus” error, so this is going to be a time-consuming diagnostic process going forward.)

The “no memory in main bus” error is not unexpected since at that moment the only boards installed in the Lambda’s backplane were the SDU and the tape controller. I have a few memory boards at my disposal, and I opted to re-install the 4mb memory board that normally resides in slot 9. Let’s run that again:
>> /tar/load
no memory in main bus
Initializing SDU
SDU Monitor version 102
>>

Well, hm. Maybe that memory board doesn’t work — let’s try the 16mb board normally in slot 12:

>> /tar/load using 220K in slot 12 load version 307 Disk unit 0 is not ready. /tar/loadbin exiting Initializing SDU SDU Monitor version 102 >>

Huzzah! The LMI has memory that works well enough to respond to the SDU, and it has a functional tape subsystem. It’s going to be awhile before I have a functioning disk, and as per the error message in the output, /tar/load expects one to be present. This is completely rational, since “load” is the program that is used to load Lisp load bands onto the disk from tape.

That’s enough for now — in the next installment, since the Lambda is now capable of loading diagnostics from tape, we’ll actually run some diagnostics! Thrills! Chills! Indecipherable hexadecimal sludge! See you next time!

At Home With Josh Part 4: High-Resolution Terminal Restoration

In my previous installment I tested the Lambda’s fans and the power supply and powered things up for the first time. A few of the fans were non-functional even after cleaning and lubricating and so an eBay order was placed. While waiting for those fans to arrive, I started taking a look at the Lambda’s monitor, referred to in the documentation variously as “High-Resolution Terminals” or “High-Resolution Monitors.” Whatever they’re called, they were in need of a bit of sprucing up:
LMI Lambda monitors, mid-cleaning

If you look closely you can see the
scarring on the picture tube’s face.

I cleaned the exterior with a bit of Simple Green and some liberally applied Magic Eraser to get some of the grungier parts off. Exposure to the elements had left some interesting etchings on the anti-glare coating on the CRT; I’m not sure if they ate it away or if they just deposited a thin layer of something on the surface– either way light scrubbing with the Magic Eraser either removed the deposits or removed the rest of the anti-glare coating to match, it’s difficult to say. Eventually the external dirt and grime were removed and the monitors looked much better.
Shiny Happy Monitor

Close-up of CRT cataracts

One of the two monitors has a CRT with “cataracts” (also referred to as “CRT Rot”) in the corners. This is a problem that plagues older televisions and monitors and is caused by degradation of the thin PVA glue layer between the front of the CRT glass and the implosion-protection lens. Over time, the PVA breaks down causing small spots to appear. The cataracts here are relatively minor; on an ADM-3A terminal I recently repaired the PVA breakdown was so extreme it had started leaking out onto the circuit boards and was an absolute bear to clean up (fortunately it’s organic so it washes off with water, but not without a fight.)

On some CRTs this can be repaired, typically by carefully separating the implosion lens from the rest of the CRT, cleaning all the PVA residue and reassembling. (Here’s an interesting write-up of one such process for old TV picture tubes.) On the Lambda’s CRTs, this is made much more difficult — there is a metal band around the tube with a “lip” that extends around the front of the tube, helping to hold the whole assembly in place. This band is glued in place with a potting compound making removal of this band extremely difficult; and due to the lip the implosion lens cannot be removed without removing this band. Fortunately the cataracts on this tube are not bad enough to warrant attempting to do this — I’m happy to put up with it — and the other monitor’s tube is free of cataracts, so far.

Inspecting the Internals

Much like with the rest of the Lambda system, we have to give the internals a thorough inspection. One of these monitors was left on top of the Lambda in the garage; the other (the one with the cataracts) was on the floor near the door and was exposed a slightly more harsh environment as a result. However, they both cleaned up very nicely on the outside so my expectation was that internally they’d be similar as well.
The interior of the monitor with the back covers removed.

Looking at the interior from the rear (as in the above photos) reveals a relatively clean monitor — though you can see some obvious rust in places like the ground strap going across the bell of the picture tube. The interior of the other monitor is very similar in terms of condition. On the left side is the monitor’s power supply, on the right is the deflection board which scans the CRT’s electron beam across the screen to form a raster, and in the middle is the “neck board”, so called because it plugs into the neck of the CRT. It supplies power to the CRT’s heaters and takes the incoming video signal from the Lambda and feeds it to the tube appropriately.

Safety First, People:

It’s important to note at this time that safety is important when working on CRTs: they tend to make use of extremely high voltages (5-10KV in monochrome tubes, up to 25KV in color sets) and you can get zapped if you’re not careful. Picture tubes can build up a charge even while sitting unplugged and unused; so even though this tube hasn’t been powered up in a couple of decades it still has the potential to bite. Discharging of the tube before working on it is a good idea, as is working with one hand behind your back (to avoid causing current flow across your heart, should you grab ground with one hand and 20KV with the other, inadvertently.)

The CRT envelope is made of glass and contains a powerful vacuum; if the glass breaks the tube can potentially implode — sending glass shards everywhere. While modern tubes (like the ones in the Lambda) have implosion protection measures in place, it never hurts to be careful around large tubes like this: watch your hands, watch your tools and make sure they don’t strike the neck of the tube where the glass is thinnest and the most likely to take damage.

The Inspection Continues:

Looking closer at the power supply you can get a better idea of the cleanup necessary here — everything is covered in a layer of dirt and shingle detritus from when the garage’s roof was replaced. Just as with the Lambda’s chassis and power supplies, I’m looking for out-of-place things and broken or damaged components. All three of these boards contain socketed chips, so checking the sockets and the ICs in them for corrosion is important. I’m also keeping my eyes open for damaged capacitors. Monitors can be hard on capacitors, especially high-resolution monitors like this one. Monitors don’t typically have fans so they tend to run hot, and heat leads to shorter lifespans of internal components.

And sure enough I found my first victims on the power supply board.
RIFA film capacitors, top view.

Exploded RIFA, from the side.
These are film capacitors, used as AC line-filters in the power supply. Or at least they were film capacitors — as you can see the casings have cracked and split and have turned a deep brown in places (they’re normally golden-yellow colored). These were manufactured by RIFA, and are absolutely notorious for failing in this way, and when they do fail they emit an unforgettable odor, though not an entirely bad one (we’ll get to those smells later). Kinda like burning paper. Which is not a coincidence because these are made of metallized paper. As they age, moisture seeps in and eventually causes a short-circuit resulting in smoke, but not usually fire. (There was this one time at the museum when one of these died in action and set off the smoke detectors and the fire department came. That was a fun day…)

Even if they haven’t already clearly failed as these have, they should be replaced as a matter of course, because they will fail if you don’t. Probably within the first thirty minutes of being powered up.
Original RIFA next to its brand-new replacement.


Moving along onto the deflection board: There are a few socketed chips, and the sockets don’t look so hot. These sockets have deeply recessed pins and my suspicion is that as a result they hold onto moisture longer, increasing the chances of corrosion. As you can see in the picture below, some of the pins show the original gold-plating, while others are green or grey. It’s likely that these sockets will provide poor contact with the IC, so I replaced it with a spare I had on-hand, a nice turned-pin socket from Mill-Max:

Bad IC socket: Before
Bad IC socket: After


On this same board I found the first instance in this restoration of a visibly-bad electrolytic capacitor:
That ain’t good…

The discovery and removal
of one bad electrolytic capacitor





















That capacitor is supposed to be a uniform silver in color. It is browned and blackened likely due to heat while in operation due to its proximity to that transformer, and it might have been a slightly under-specced part as well. Instant candidate for replacement, no questions asked.

On the neck board we find another kind of capacitor that can often cause issues; look closely at the four blue raindrop-shaped components in the below picture:

One of these things is not like the others.

Well, they’re all supposed to be blue, but the second one from the left is black and sure enough it’s a dead short, rather than a capacitor. These are tantalum capacitors and they have a tendency to explode in a tiny little fireball when they go bad — and they can scorch other components when they do so. And the smell they make is decidedly unpleasant. Given the state of the black one it seemed prudent to replace all four just to be on the safe side. Takes a long time to get that odor out of an already stuffy basement, I’m not taking any chances.

There is one further board in these monitors, called the “headboard” — it lives in the monitor stand and breaks out the signals on the cable from the Lambda into keyboard, mouse, and video. It also includes a tiny speaker and three controls for brightness, contrast, and volume:

Ugh. Just, ugh.

The one in the monitor that had been sitting on top of the Lambda was just a bit dusty, but the one that’d been on the floor… yow. Some serious insect activity in here over the years, and everything was pretty well covered in… insect stuff. I took the board out of the housing and scrubbed the base-plate down in the utility sink. I went over the PCB with a soapy toothbrush and Q-Tips to get as much gunk off as possible. It cleaned up pretty well!

Ahh, much better.




Having assessed the condition of the boards (and having gone through and cleaned everything as thoroughly as possible), I made the decision to do a complete “re-cap” of the three main boards in both monitors: a replacement of all of the electrolytic capacitors and the problematic-looking tantalums. I placed an order for replacement parts (I tend to use Mouser or Digi-Key for this sort of thing) and 3-5 days later a box of capacitors arrived on my doorstep.

Replaced tantalum capacitors on the neck board.

At this point it’s a straightforward matter: desolder the old components, and solder in the new ones, one at a time. I have a Hakko desoldering iron (just like the ones we use at work) and a Weller soldering station that have served me well over the years. I didn’t take any pictures of the actual desoldering/resoldering process because I only have two hands and I don’t own a tripod… I’m lame.

All the replaced capacitors from the power supply board, next to the re-capped supply. On a really ugly benchtop.


Woo-hoo!
With everything reassembled in the first monitor, the only thing left to do was to put it on the bench, plug it in, cross my fingers, and turn it on. I wasn’t entirely sure it would do anything without being hooked up to a running Lambda with functioning video hardware: some monitors of this era won’t light up unless they’re getting sync pulses from their video input (Sun-3 monochrome workstation monitors for example). Others will display a “free-running” blank raster instead. Turns out the Lambda console is one of these latter:

I got very lucky and things appeared to be working as perfectly as could be determined without a valid video signal to feed it. I let it burn in on the bench for a half an hour and no issues arose. If you’ve accidentally put an electrolytic capacitor in backwards, you’ll know within the first few minutes, if not sooner… (another fun smell you don’t want in your house.)

The next day I took on the second console, going through exactly the same steps — like deja vu all over again. However, I wasn’t as lucky with this one; no smoke or fire but also no action on the display at all, and no faint chatter of the yoke indicating deflection, no static on the face of the tube indicating the presence of high voltage. The neck of the picture tube lit up, however — so at least a few things were functional. The voltages coming out of the power supply (it generates +48V and +32V) were in the right ballpark at +45 and +33. There is a potentiometer on the power supply to adjust these voltages, so I gave it a small tweak to get closer to +48V and at that point I heard the HV kick into gear, but I don’t understand why — the voltages were a little off but not enough to prevent the deflection board from running, and I’d only tweaked it up to +46V anyway. This seems like a sign of a bad connection: a loose wire, dirty connector, or maybe a cold solder joint. At this point I had high voltages and could hear evidence of deflection but there was nothing on the display, no free-running raster like on the first monitor.

I powered it down and took a closer look at everything; cleaned the various cables and connectors on the power supply and inspected my soldering job — still nothing jumped out at me as being obviously wrong. But I put it back together and it was still working as before, deflection running and high voltages being generated, though I was still getting nothing on the display at all. At this point I needed a break and decided to shelve the second monitor for the time being. One working display was enough to use with the Lambda (assuming I ever did get it to do anything) and at that point I’d return to debugging the other.

In my next write-up I’ll see if I can get the Lambda to load and run diagnostics from the world’s slowest 9-track tape drive, after dealing with a minor setback. The anticipation, you can hardly stand it!